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Allison T-40 : ウィキペディア英語版
Allison T40

The Allison T40, company designation Allison Model 500, was an early American turboprop engine composed of two Allison T38 power sections driving a contra-rotating propeller via a common gearbox.〔
==Design and development==

The T40 concept originated at Allison in 1944, where design studies were carried out on a turboprop engine. Taking advantage of this effort, the US Navy awarded Allison a contract for the design and development of a turboprop engine. The resulting T40 combined two Allison T38-A-1 power sections side-by-side with a common reduction gearbox powering a contra-rotating propeller. Similar in layout to the Armstrong Siddeley Double Mamba, the T40 differed in that each engine drove both the forward and the rear propellers, unlike the Double Mamba, where each Mamba power section drove either the front or the rear propeller separately.
The T38-A-1 power sections each contained 17-stage compressors giving a pressure ratio of 6.3:1, eight combustion chambers, and four-stage turbines. A combining reduction gearbox was driven via extension shafts from the power sections. Each transmission shaft incorporated a clutch to allow the power sections to be run independently.〔
Accessories included a Master Control Unit, mounted above the compressors; and an air driven starter on the gearbox. The compound reduction gear had an overall reduction ratio of 15.75:1 and incorporated an airscrew brake to prevent windmilling when the engine was stopped. Anti-icing for the air intakes was supplied by compressor bleed air. The contra-rotating propeller consisted of two three-bladed Aeroproducts propellers fitted to concentric shafts.〔
Testing of the XT40 began on 4 June 1948, revealing some major vibration problems from the reduction gearbox due to mis-matched noise frequencies caused by poorly designed gear teeth. The de-coupling system, designed to disconnect a power section in the event of failure worked successfully. During a run in a test cell one power section developed a major oil leak and an attempt to shut it down failed because the engine carried on running on the leaking oil. After many attempts to shut it down the offending power section could only be shut down by destroying the compressor with buckets of nuts and bolts thrown down the intake, proving the de-coupling system.〔
First flight test of the T40 was in the Convair XP5Y flying boat on 18 April 1950 fitted with four T40-A-4 developing . Service use of the T40 revealed problems with integrity of the propellers and gearboxes with at least one instance each of a propeller breaking free and a gearbox separation. One unusual problem was discovered during ground running of the Republic XF-84H Thunderscreech turboprop powered fighter; the special transonic 3-bladed single propeller set up harmonics that proved to be harmful to humans within a certain distance from the aircraft.〔
The major problems of the T40 were its fragile gearbox, and the propeller control system which used 25 vacuum tubes, and was far from reliable. As the individual power plants were clutched into the gearbox, it was intended in most instances that the aircraft could cruise on one half of the engine and only engage the second power-section when there was need. In practice the system did not work well. Failure to recognize that one of the T38s had failed, and its compressor was devouring power produced by the other section, led to the loss of the first prototype Douglas XA2D-1 and its pilot on 14 December 1950.〔

抄文引用元・出典: フリー百科事典『 ウィキペディア(Wikipedia)
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